alaska airlines flight 261 crash video


And hes just hit the water, said one pilot. The threads eventually lost up to 90% of their thickness, compared to 22% at the maximum wear depth of one millimeter. But maintenance, poorly done, will find a way to bite somewhere else. It aggressively took action to improve itself by hiring a new vice president (VP) of safety who reported directly to the CEO, filling executive vacancies in safety and maintenance, creating a large safety office, hiring 130 new mechanics, revising its general maintenance manual and reviewing every C-check aircraft in the fleet to ensure that all work was properly performed. Ameet Prasad lost his younger brother . At 15:55, the dispatcher returned with wind speeds, wind directions, and runway conditions at San Francisco and Los Angeles. [38] Many residents of Seattle had been deeply affected by the disaster. It added dozens of new routes, expanded to a large number of new cities, and even added services to Mexico in order to offset the seasonal nature of its flights to Alaska. ?On January 31, 2000, about 1621 Pacific standard time, Alaska Airlines, Inc., flight 261, a McDonnell Douglas MD-83, N963AS, crashed into the Pacific Ocean about 2.7 miles north of Anacapa Island, California. It really wants to pitch down., Alaska two six one, said the controller, Say your condition?, Two six one, we are at 24,000 feet, kinda stabilized, said Thompson. So theyre trying to put pressure on you, said Tansky. In December of 1998 the federal government launched a criminal investigation into Alaska Airlines, seizing documents and interviewing witnesses. I need everything picked up and everybody strapped down, he said, cause Im gonna unload the airplane and see if we can gain control of it that way. His intention was to fly at lower speeds where there would be less aerodynamic force pushing up on the stabilizer. There was nothing that Tansky and Thompson could have done to control the airplane. I didnt want to call you guys, said the flight attendant, but that girl theyre like, you better go up there and tell them., I need you strapped in, dear, said Thompson, cause Im going to release the back pressure and see if I can get it back.. But after Liotine left for the night, the next shift and the shift supervisors decided to run the test again before taking his measurement at face value. [6] The accident showed that certain wear mechanisms could affect both sets of threads and that the wear might not be detected. [6]:195197, At 16:09 (00:09 UTC), the flight crew successfully used the primary trim system to unjam the stuck horizontal stabilizer. Uh, you getting full nose trim down but are you getting any you dont get no nose trim up, is that correct? maintenance asked. An FAA inspector who reviewed the 1996 extension said that the airline presented only Boeings recently extended lube interval as justification. Neither the electric switches (which the pilots called pickle switches) nor the fully manual trim handles (referred to as the suitcase handles) could move the stabilizer. However, several factors led the board to question "the depth and effectiveness of Alaska Airlines corrective actions" and "the overall adequacy of Alaska Airlines' maintenance program". A flight traveling from Mexico crashed into the Pacific Ocean on Jan. 31, 2000. The design of the jackscrew on the MD-80 series was identical to that of the original 1960s-era Douglas DC-9, which was certified to meet requirements stating that no reasonably probable single failure of the control system could jeopardize the controllability of the airplane. On board flight 261, Captain Thompson vented to First Officer Tansky: Drives me nuts, he said. Note: this accident was previously featured in episode 2 of the plane crash series on September 16th, 2017, prior to the series arrival on Medium. My group and I were stunned to see that the acme nut was not attached to the jackscrew. [6], Between 1985 and 1996, Alaska Airlines progressively increased the period between both jackscrew lubrication and end-play checks, with the approval of the Federal Aviation Administration (FAA). All passengers were identified using fingerprints, dental records, tattoos, personal items, and anthropological examination. Air Alaska Flight 261 dives into the ocean shortly after takeoff, killing the 88 passengers and crew on board. As investigators recovered more and more of the plane from the ocean floor, a troubling picture of the sequence of events began to emerge. It was no wonder, given these findings, why Alaska Airlines mechanics didnt know how to grease the jackscrew, and why nobody held them accountable for not doing so properly. The stabilizer is attached to a giant threaded screw, called the jackscrew, which feeds through a nut attached to the aircraft structure inside the tail. Aviation accident over the Pacific Ocean in 2000, Inadequate lubrication and end-play checks, A block of altitudes assigned by ATC to allow altitude deviations. He's, ah, down. citizens. [26], The investigation then proceeded to examine why scheduled maintenance had failed to adequately lubricate the jackscrew assembly. [31] The sundial casts a shadow on a memorial plaque at 16:22 each January 31. Yeah, we tried everything together, said Thompson. The 88 passengers and crew members aboard Alaska Airlines Flight 261, which crashed off the coast of Ventura County on Jan. 31, 2000, will not soon be forgotten. (To avoid confusion, from here on out nose up and nose down, as they relate to the pitch of the airplane, will be used to describe the stabilizers direction of motion. Once the thread had failed, the horizontal stabilizer assembly was subjected to aerodynamic forces that it was not designed to withstand, leading to the complete failure of the overstressed stabilizer assembly. During the course of the investigation, and later in its final report, the NTSB issued 24 safety recommendations, covering maintenance, regulatory oversight, and aircraft design issues. Increasing the interval between lubrications meant that every lubrication had to be done correctly in order to prevent accelerated wear and tear. [3][4], The pilots of Flight 261 were both highly experienced aviators. Both of these circumstances resulted from Alaska Airlines' attempts to cut costs. Almost all of these recommendations were implemented. After months of constant movement back and forth, the tests showed normal wear rates with both grease types. [6], Beginning at 16:19 (00:19 UTC), the CVR recorded the sounds of at least four distinct "thumps", followed 17 seconds later by an "extremely loud noise", as the overstrained jackscrew assembly failed completely and the jackscrew separated from the acme nut holding it in place. Flying Inverted | Cutting Corners | Alaska Airlines Flight 261 | 4K TheFlightChannel 1.43M subscribers 1.7M views 4 years ago Find out why this Alaska Airlines MD-83 crashed into the. It began life as a regional airline in Alaska, and by the time deregulation arrived in the late 1970s, it only had one destination in the lower 48 states. Lets do that. Thompson attempted to move the stabilizer trim using either the electrical switches, the trim handles, or both, in an effort to clear the jam. [6], Using side-scan sonar, remotely operated vehicles, and a commercial fishing trawler, workers recovered about 85% of the fuselage (including the tail section) and a majority of the wing components. Join the discussion of this article on Reddit! Laboratory tests indicated that the excessive wear of the jackscrew assembly could not have accumulated in just the four-month period between the September 1999 maintenance and the accident flight. Weve run just about everything. The 2 pilots, 3 cabin crewmembers, and 83 passengers on board were killed, and the airplane was destroyed by impact forces. [25] Ultimately, the lack of lubrication of the acme-nut thread and the resultant excessive wear were determined to be the direct causes of the accident. As the NTSB investigation continued, so too did the criminal investigation and the saga of John Liotine. They had run out of altitude. The FAAs special inspection report noted that the position of Director of Maintenance had gone unfilled since 1998; the Director of Operations position was empty; the Director of Safety was also the Director of Quality Control and the Director of Training and didnt report to high-level management; there was no maintenance training curriculum; on-the-job training was completely unstructured; the procedures in use didnt match those outlined in the maintenance manual; planes had been released from C-checks with paperwork incomplete; perishable and consumable materials had expired; shift turnover paperwork was missing, unsigned, or incomplete; work cards were not filled out properly; and more the list went on and on. A flight attendant opened the cockpit door, and Captain Thompson briefed her on the situation. [6]:1011 First Officer William "Bill" Tansky, 57, had accumulated 8,140 total flight hours, including about 8,060 hours as first officer in the MD-80. The leading edge of the stabilizer can be raised or lowered as it pivots about a rear hinge point. Were slowing here, and were gonna do a little troubleshooting, can you give me a block altitude between twenty and twenty five?. Holy shit, said Thompson, pulling back hard on the controls. The block-on-ring test rigs were lubricated with grease where they made contact. In NTSB board member John J. Goglia's statement for the final report, with which the other three board members concurred, he wrote: This is a maintenance accident. The metal from which the jackscrew is made is ever so slightly harder than the metal used in the nut. At this contact, the ring slowly wore a divot into the surface of the block. The first hour and a half was smooth flying: at 3:55 p.m. the. The lead mechanic that day was John Liotine, a rare Alaska Airlines employee who still took safety seriously. Following the crash, families successfully lobbied for design changes and improved airplane maintenance requirements. An engineering fix developed by engineers of NASA and United Space Alliance promises to make progressive failures easy to see and thus complete failures of a jackscrew less likely. For the relatives of the victims, this fact made it all the more important that Alaska Airlines pay for its negligence. Only by applying a continuous maximum nose up elevator input on his control column, a task which required enormous physical effort, was Captain Thompson able to maintain level flight. Captain Thompson argued that conditions would be more suitable for landing at Los Angeles, and the dispatcher admitted that the reason they preferred San Francisco was because a diversion would disrupt flow, worsening mounting delays in Alaskas flight schedule.

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